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Technical Paper

Achievement of Low Emissions by Engine Modification to Utilize Gas-to-Liquid Fuel and Advanced Emission Controls on a Class 8 Truck

2005-10-24
2005-01-3766
A 2002 Cummins ISM engine was modified to be optimized for operation on gas-to-liquid (GTL) fuel and advanced emission control devices. The engine modifications included increased exhaust gas recirculation (EGR), decreased compression ratio, and reshaped piston and bowl configuration. The emission control devices included a deNOx filter and a diesel particle filter. Over the transient test, the emissions met the 2007 standards. In July 2004, the modified engine was installed into a Class 8 tractor for use by a grocery fleet. Chassis emission testing of the modified vehicle was conducted at the National Renewable Energy Laboratory's (NREL) Renewable Fuels and Lubricants (ReFUEL) facility. Testing included hot and cold replicate Urban Dynamometer Driving Schedule (UDDS) and New York Composite (NYComp) cycles and several steady-state points. The objective of the testing was to demonstrate the vehicle's with the modified engine.
Technical Paper

Regulated Emissions from Biodiesel Tested in Heavy-Duty Engines Meeting 2004 Emission Standards

2005-05-11
2005-01-2200
Biodiesel produced from soybean oil, canola oil, yellow grease, and beef tallow was tested in two heavy-duty engines. The biodiesels were tested neat and as 20% by volume blends with a 15 ppm sulfur petroleum-derived diesel fuel. The test engines were a 2002 Cummins ISB and 2003 DDC Series 60. Both engines met the 2004 U.S. emission standard of 2.5 g/bhp-h NOx+HC (3.35 g/kW-h) and utilized exhaust gas recirculation (EGR). All emission tests employed the heavy-duty transient procedure as specified in the U.S. Code of Federal Regulations. Reduction in PM emissions and increase in NOx emissions were observed for all biodiesels in all engines, confirming observations made in older engines. On average PM was reduced by 25% and NOx increased by 3% for the two engines tested for a variety of B20 blends. These changes are slightly larger in magnitude, but in the same range as observed in older engines.
Technical Paper

Interlaboratory Cross-Check of Heavy-Duty Vehicle Chassis Dynamometers

2002-10-21
2002-01-2879
Six laboratories capable of chassis-testing heavy-duty vehicles participated in a crosscheck program designed to compare emissions results from a Ford L-9000. The single-axle vehicle was shipped to each laboratory and tested through a series of UDDS and steady-state cycles. The resulting data were compared statistically using reproducibility and repeatability analyses. Although one lab produced some results that significantly differed from the other five, the remaining labs produced comparable results. TPM, CO and THC were the most variable while NOX and CO2 were most stable. Lab differences included atmospheric and environmental conditions, road-load curve application and drivers. Comparison of steady state and transient tests suggest that driver variability is not a major factor.
Technical Paper

A New Method for Diesel HC Collection and Speciation

2000-10-16
2000-01-2951
As interest in diesel emissions has grown, so has the importance of analyzing the components of the exhaust. These compounds include alkanes, aromatics and alkenes, ranging in carbon number from C1 - C24, and polycyclic aromatic hydrocarbons (PAHs). These hydrocarbons can be in gaseous, semi-volatile and particulate form and cannot be collected accurately by conventional Tedlar™ bag sampling due to deposition of condensing vapor on bag walls. There are some sorbent methods used currently for the speciation of this exhaust, which require either thermal desorption and/or solvent extraction equipment. Automotive Testing Laboratories, Inc. (ATL) reports here on the use of a gas chromatography (GC) method designed to specifically look at hydrocarbons in the diesel (C9 - C24) range.
Technical Paper

Exhaust Emissions and Combustion Stability in a Bi-Fuel Spark Ignition Engine

1995-02-01
950468
A Saturn 1.9 liter engine has been converted for operation on either compressed natural gas or gasoline. A bi-fuel controller (BFC) that uses closed-loop control methods for both fuel delivery and spark advance has been developed. The performance and emissions during operation on each fuel have been investigated with the BFC, as well as the performance and emissions with the stock original equipment manufacturer (OEM) controller using gasoline. In-cylinder pressure was measured at a rate of 1024 points per revolution with piezoelectric pressure transducers flush-mounted in the cylinder head. The in-cylinder pressure was used in real time for ignition timing control purposes, and was stored by a data acquisition system for the investigation of engine stability and differences in the combustion properties of the fuels.
Technical Paper

The Design of a Bi-Fuel Engine Which Avoids the Penalties Associated with Natural Gas Operation

1995-02-01
950679
An alternative fuel that has demonstrated considerable potential in reducing emissions and crude oil dependence is compressed natural gas (CNG). A dedicated CNG vehicle suffers from the lack of an adequate number of fueling stations and the poor range limited by CNG storage technology. A vehicle capable of operating on either gasoline or natural gas allows alternative fuel usage without sacrificing vehicle range and mobility. Although many such bi-fuel vehicles are in existence, historically they have employed older engine designs and made compromises in engine control parameters that can degrade performance relative to gasoline and increase emissions. A modern production engine, a 1992 Saturn 1.9 liter 16 valve powerplant, is being optimized for operation on each fuel to realize the full potential of CNG in a bi-fuel system. CNG operation in an engine designed for gasoline typically suffers from reduced power, due in part to displacement of air by gaseous fuel.
Technical Paper

Turbocharging a Bi-Fuel Engine for Performance Equivalent to Gasoline

1994-10-01
942003
A bi-fuel engine capable of operating either on compressed natural gas (CNG) or gasoline is being developed for the transition to alternative fuel usage. A Saturn 1.9 liter 4-cylinder engine was selected as a base powerplant. A control system that allows closed-loop optimization of both fuel delivery and spark timing was developed. Stock performance and emissions of the engine, as well as performance and emissions with the new controller on gasoline and CNG, have been documented. CNG operation in an engine designed for gasoline results in power loss because of the lower volumetric efficiency with gaseous fuel use, yet such an engine does not take advantage of the higher knock resistance of CNG. It is the goal of this research to use the knock resistance of CNG to recover the associated power loss. The two methods considered for this include turbocharging with a variable boost wastegate and raising the compression ratio while employing variable valve timing.
Technical Paper

A Controller for a Spark Ignition Engine with Bi-Fuel Capability

1994-10-01
942004
A bi-fuel engine with the ability to run optimally on both compressed natural gas (CNG) and gasoline is being developed. Such bi-fuel automotive engines are necessary to bridge the gap between gasoline and natural gas as an alternative fuel while natural gas fueling stations are not yet common enough to make a dedicated natural gas vehicle practical. As an example of modern progressive engine design, a Saturn 1.9 liter 4-cylinder dual overhead cam (DOHC) engine has been selected as a base powerplant for this development. Many previous natural gas conversions have made compromises in engine control strategies, including mapped open-loop methods, or resorting to translating the signals to or from the original controller. The engine control system described here, however, employs adaptive closed-loop control, optimizing fuel delivery and spark timing for both fuels.
Technical Paper

Performance of a High Speed Engine with Dual Fuel Capability

1994-03-01
940517
Concern over dwindling oil supplies has led to the adoption of alternate fuels to power fleet vehicles. However, during the interim period when alternate fuel supply stations are few and far between, dual fuel engines prove a necessity. In the light duty arena, these engines are typically gasoline engines modified to accommodate compressed natural gas (CNG) as an alternate fuel, but they are seldom optimized with both fuels in mind. A Saturn 1.9 liter 4 cylinder dual overhead cam engine was selected as a base for developing an optimized gasoline/CNG powerplant. Baseline data on power and steady state emissions (CO2, CO, NOx, HC) were found using the standard Saturn controller. In addition to monitoring standard sensor measurements, real-time pressure traces were taken for up to 256 cycles using a modified head with embedded PCB piezoelectric pressure transducers.
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